Root Cause Analysis (RCA)

Reformer Fan Bearing Change Times cut by 90%

Root Cause Analysis (RCA) provides a solution to Reformer Fan Bearing Change Times cut by 90%.

Article Type:Root Cause Analysis (RCA)
Category:Mechanical
Equipment Type:Miscellaneous Rotating Machine Problems
Author:S. Raghava Chari

Note: This root cause analysis (RCA) is from real-time scenarios that happened in industries during the tenure of two or three decades ago. These articles will help you to improve your troubleshooting skills and knowledge.

Fan Bearing Change Times cut by 90%

Unbolt the over 250 Nos. 10 mm dia casing bolts

Position a crane suitably before plant shutdown (SD), after SD lift the casing upper half (above figure), place it nearby; lift the rotor 20 mm using a chain pulley block suspended from crane hook for Antifriction bearings (AFB) pull out; change the failed AFB, assemble back, etc.

Author Solution

Though the crew assured the instruction manual offered no easier bearing changing method, the author felt designers would have envisaged an easier bearing changing method:

Reformer Fan Bearing Change Times cut by 90%

He carefully viewed the fan 10 minutes and suggested to replace the AFBs thus:

  1. Arrange bearing pullers and electric bearing heaters close by before fan SD.
  2. Unbolt both side Pillow Block’s upper halves
  3. Unbolt both sides the top ½ ring bolted to the fan entry filter
  4. Lift the fan rotor with a crane carefully and slowly till it contacts the casing top; the rotor tip to case bore distance is usually sufficiently large and bearing OD will be clear the pillow block step
  5. With the crane holding the rotor, replace both the bearings.
  6. Lower the rotor carefully and guide both end AFBs into the pillow block seat
  7. Mallet tap the shaft and seat the both end AFBs in the pillow block
  8. Tighten Pillow Block top halves. The fan is ready for use! Just 2 hours task- not 2 shifts i.e., 16 hours.

The study-based solution Benefits

The plant resumed full capacity production within 3 hours and with just a few easy maintenance efforts and needless 13 hours ½ capacity runs.

Author: S. Raghava Chari

Do you face any similar issues? Share with us through the below comments section.

If you liked this article, then please subscribe to our YouTube Channel for Instrumentation, Electrical, PLC, and SCADA video tutorials.

You can also follow us on Facebook and Twitter to receive daily updates.

Read Next:

You've successfully subscribed !
Share

Recent Articles

  • PLC Tutorials

VFD Simulator Download – Free Yaskawa V1000 Software

VFD simulator download: Master the online tool from the Yaskawa V1000 & programming software for…

2 days ago
  • PLC Tutorials

Conveyor Sorting Machine PLC Program with Calculation Function

The conveyor sorting machine is widely used in the packing industries using the PLC program…

6 days ago
  • PLC Tutorials

Example of Flip-Flop PLC Program for Lamps Application

Learn the example of flip-flop PLC program for lamps application using the ladder logic to…

6 days ago
  • PLC Tutorials

STAR DELTA Programming using PLC Controller

In this article, you will learn the STAR DELTA programming using PLC controller to start…

6 days ago
  • Instrumentation Design

Single and Three Phase Immersion Electrical Heaters Wiring Circuits

Lube oil consoles of rotary equipment packages in industrial process plants are usually equipped with…

3 days ago
  • Instrumentation Design

Immersion Heaters in Lube Oil Consoles

Rotating equipment packages such as pumps, compressors, turbines need the lube oil consoles for their…

6 days ago